Commit d9320af3 authored by Akinobu Mita's avatar Akinobu Mita Committed by Greg Kroah-Hartman

iio: adc: ti-ads1015: don't return invalid value from buffer setup callbacks

commit a6fe5e52 upstream.

pm_runtime_get_sync() and pm_runtime_put_autosuspend() return 0 on
success, 1 if the device's runtime PM status was already requested status
or error code on failure.  So a positive return value doesn't indicate an
error condition.

However, any non-zero return values from buffer preenable and postdisable
callbacks are recognized as an error and this driver reuses the return
value from pm_runtime_get_sync() and pm_runtime_put_autosuspend() in
these callbacks.  This change fixes the false error detections.

Cc: Daniel Baluta <daniel.baluta@gmail.com>
Signed-off-by: default avatarAkinobu Mita <akinobu.mita@gmail.com>
Signed-off-by: default avatarJonathan Cameron <Jonathan.Cameron@huawei.com>
Signed-off-by: default avatarGreg Kroah-Hartman <gregkh@linuxfoundation.org>
parent 1c68b99a
...@@ -235,7 +235,7 @@ static int ads1015_set_power_state(struct ads1015_data *data, bool on) ...@@ -235,7 +235,7 @@ static int ads1015_set_power_state(struct ads1015_data *data, bool on)
ret = pm_runtime_put_autosuspend(dev); ret = pm_runtime_put_autosuspend(dev);
} }
return ret; return ret < 0 ? ret : 0;
} }
static static
......
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